I was out this morning and put in an hour. That makes it 38.2hr in Phase I, so a couple more hours and I’m free from my box. Everything has been going well. The only minor issue I was battling over the last couple weeks is the camber of the pilot-side main gear wheel. After […]
20th test flight
We’ll I’m just over 20hrs now, half way. I have most of the major issues taken care off. The engine is running cool, no oil leaks, oil vent ported to exhaust. This flight I took off the sparrow strainer and trim at high speed was much better. Before, at 160kts, I ran out of trim […]
13th test flight
In attempt to correct high CHT in #3 cylinder, I went at the cooling plenum again. This time, opening up the area fore of cylinder 3 trying to make the turn down from the runner from the NACA to cylinder #3 a little more gradual. Before going at it, the plenum was up tight along […]
8/9/10th test flights
On the 7th flight, I continued to see high CHT’s this time #2, so I thought I might have a fuel distribution problem. I took all the injectors out and cleaned them, then switched them around until I measured equal fuel flow thru all cylinders (injectors out of the cylinders and attached to the lines […]
7th test flight
With a better roll trim and improved engine cooling plenums to provide better airflow to cylinders 3/4, I took her for another flight. There were broken clouds down to ~4000′, so I climbed up to 10,000′ to get on top. First off, I noticed the improved roll trim out of the gate. I could now […]
6th test flight
In attempt to figure out the plane’s left roll tendency, I picked up a digital level at Harbor Freight this morning, leveled the plane and started comparing angles between the wings. No matter where I measured, they were very close, within 0.3deg. I put the level parallel to the longitudinal axis of the plane and […]
5th test flight
Today I spent the morning taking care of a list of squawks. First, I found an oil leak in the engine. One of the cylinder drain tubes was leaking from where it joins to the cylinder. I took off the tube and discovered that it was cracking right at the base of the flare for the […]
4th test flight
On the third test flight, once I climbed to 5000′ and brought it up to speed, I noticed a definite roll tendency. To see if I could correct this, I drooped the ailerons so their trailing edges were 1/8″ below the wing at rest/level. During this test flight, tho, it still wanted to roll left […]
3rd flight
I took it out today for a bit longer flight. I took off from KORH on 29, stayed in the pattern for one round to ensure everything was ok, then headed, climbing out west. I climbed to 5000′ (got there pretty quick, too), then after going out 15mi from the airport, setup a race track […]
Second flight
I had a few things to take care of after the first flight. Right after that flight, I jacked the plane up and found why the gear was not retracting properly – newly inflated tires not fitting into wheel wells. I opened up the wheel wells so they fit in easily at 55psi and also […]